det nightmare [Archive] - SR20 Forum

: det nightmare


Ryshe
09-28-2002, 05:44 PM
Before I go any further in typing anything else, I just want to start off stating that I am not trying to flame BoostFactor in anyway, but I have to list the facts so that I can get appropiate answers. This is going to be a long post just to warn you ahead of time. I've run out of options and ideas and BoostFactor doesnt seem to have a solution other than for me to chisel out more cash, so to the forums I have come.

I recently got a s13 sr20det blacktop swapped into my 1995 240sx by BoostFactor. I will *** go in order of events by sections and the current issues we resolved one by one to try and get my car running normally.

To start off, I thought I had paid for a complete swap but this is what my car came out as :
-Swapped in Engine/Tranny + Wiring + Hosing , etc.
-Jim Wolf ECU
(Yep, if you're looking for more items....that's it, no sidemount intercooler, no proper plug wires, no downpipe, the list goes on)

1st Time I got car back from BF
Story : My car had a pretty noticeable exhaust leak when I first turned it on. I drove it around easy while doing test runs, and it seemed to be ok other than the loud exhaust noise so I took it back home. On the drive home, I noticed it felt really weak and the temperature levels were unstable, so I pulled in to the local pep boys around my area and just as I did that, my radiator hose came loose along with the plastic inlet and out went all my coolant. Luckily the Pep Boys mechanic was cool and helped me find a new better fitting hose and some new clamps and we got it back on as tight as we could but he warned me that it could come off again since the lip was gone. Later that night we took the car out for some more test driving and found that at full throttle, sometimes even half, once the rpms hit 3000, it would basically hover there or crawl up slowly and the engine would *** sputter during this. I didnt push the car like this until that night because I was trying to drive it nice when I first took it back home. So we went back and did a full checkup on the car, took pictures, and made a video, but I won't release any of it for now because BoostFactor did fix, as promised, a lot of the things that were wrong that I had documented. If you want the details then you can talk to me through e-mail or private messages.

Issues:
- Radiator hose came off because the plastic inlet on my stock radiator was cracked due to the clamp being clamped down too hard on improperly sized hosing.
- Intake Piping + Turbo piping to Throttle body kept blowing loose at high boost ( BoostFactor later found that this was due to a bad BOV that I had bought on Ebay ).
- Excessive engine noise due to exhaust leak.
- Oil Pan was dented real bad.
- Plugs did not fit snugly.
- Car is running very very rich.
- Had trouble making it past 3k rpms.

After some Fixes
Story: Seeing that my car could not even considered to be working properly, my friends and I went about trying to fix such things as plugging up leaks in the intake system, tightening hose clamps, adding a boost gauge, and adding a Pop Charge Cone Filter....yes you guessed it, I didn't have a filter either. So we took it out for another test run after these minor modifications and found it worked much nicer and was able to make it past 3k rpms. However now it would start the stuttering and sputtering at around 5500 rpms at full throttle. And so, finding no real solutions, I made a list of all the problems and brought the car back to BoostFactor.

New Observed Issues:
- Engine was overheating very easily.
- Windshield wiper blades went off randomnly even though they were turned off
- Reverse lights did not work
- Car can now make it to 5k rpms
- Feels very very weak in general as far as HP.

2nd time I got car back from BF
Story: I was much happier this time upon receiving my car as now you could say my car was functioning fairly normally. It felt a lot stronger but was obviously still not up to par. The BOV was replaced, welded piping was made for the intake piping, a downpipe was added, new properly fit plug wires except for one, new spark plugs/distributor/cap and the other issues were all attended to. I drove it home again nicely, not pushing it too hard and we commenced trying to figure out why the car was still running weak and surging. The car actually goes through the entire rpm band now, but still runs in my opinion, quite poorly. The idle at this point would keep jumping after you rev up from 1000 and sit at an avg of 1500 rpms consistently. A lot of the old issues have been resolved up to this point, so here's the new list of the new known issues at this point.

New Issues List:
- Car Idle is inconsistent
- 4500-6000 rpm band surges and is unstable. Feels like no power at all
- Engine still overheating
- Transmission makes weird noises whenever the car is moving in any gear. Noise goes away when clutch is pushed in or if in neutral.
- Reverse lights now continuously on. They never turn off.
- Windshield wipers went on and could not get them to turn off
except finally I pulled the fuse to make them stop. =\
- Boostleak where we T'd off the vacuum tube for Boost Gauge hookup. (this *** my own fault but I fixed the problem)
- Car ran pretty much as fast as my stock KA24 motor did at this point. sad....yes....very sad.....

After some more Moddage
Story: I drove the car for the next few days, performing checkups every night and eventually refilling my radiator with a better mixture. We also added a switch to keep the fan constantly running. This seemed to stop the overheating problem but the very next day as I was driving home from school, the dreaded hose came off again and once again....no more fluids and a very overheated car. We glided back to my place since it *** really close and dismantled the radiator, and did some more checkups on the car such as wiring, spark plugs, etc. We had not checked the spark plugs ourselves ever up to this point so we were surprised to find them sitting loose, and improperly gapped at .04 instead of .03. We fixed that and the next day, which would be yesterday now..., I called around looking for replacment radiators and ended up buying a used stock s13 jspec radiator from BoostFactor. I also learned from BoostFactor that the sputtering that was still occurring between 4500 rpms and 6000 rpms could be because my stock fuel pump was still being used.... ... no comment... Yah, but anyhow I figured it made sense that the engine would start sputtering like due to lack of fuel when the throttle was at 100%, so I went to the Nissan Dealership that same day and picked up a 300zx TT Fuel Pump. I went back and installed the new Fuel Pump accordingly, using the stock filter pickup and making sure it fit snug. Had to do some adapting but it installed nicely. The jdm radiator was put on as well, with a couple trips to auto stores to get new hosing, clamps, plugs, etc. We had to custom mount it since the mounting brackets and screw holes didnt match up correctly, but we eventually got it on nice and tight with the fan attached to it. So we put everything back together, double checked everything, added the coolant, crossed our fingers, and started her up. The car sounded like it was about to die at first as it was adapting to the new fuel pump, but it smoothed out quickly and idled nicely at 1000 rpms. It wasn't long before we noticed the radiator...go figure.....was leaking all over the place, but it was leaking it out slow enough that we could take the car out for a test run without risk of over heating. So I drove the car out on the streets, praying to God that it would haul some ass like it was supposed to.....put the pedal to the ground......and.....nothing... It went smoothly up the rpm band all the way to 7k with slight surges, but it felt like the car was even weaker than before, which we later confirmed. And that should bring us up to date to my current nightmare of trying to get my car to run properly. And so here's a new list of problems and current fixes applied.

Concluding Issues and Observations:
- Overheating problem was addressed and fixed, but a new aftermarket radiator will be needed and I have that ordered and on the way. I'll *** have to deal with refilling my radiator with water every few miles until it comes. =\
- Car is running weaker than before we applied the mods/fixes in the above story.
- RPM band is now fairly smooth, but still surges sometimes.
- Idle is fairly normal at steady 1k rpms now.
- Still running extremely rich with enormous amounts of backfiring.
- There are no known boost leaks in the intake piping, etc. Dunno if there may be a leak in the wastegate or *** not.
- Still haven't resolved the issue on "continuously on" reverse lights and windshield wipers.
- Transmission still makes continuous noise when in gear.
- Wiring and plugs SHOULD be all done correctly....but...who knows. Everything that's needed seems to be plugged in.

Current List of Mods
*if anything isn't listed, then assume it's stock.*
- Pop Charger Cone Filter
- 300zx TT Fuel Pump
- Blitz Super Sound BOV (atmospheric)
- 3" Downpipe
- 3" Cat-Back Piping
- 3 Jim Wolf fitted Plug Wires, 1 Stock Plug Wire (fits in, *** stick out *** it's too long)
- New Spark Plugs (.03 gap)
- New Distributor/Cap
- Welded Intake Piping that doesnt blow off or leak
- JDM Stock Leaky Radiator
- Manual Switch on/off for Fan
- Accurate Boost Gauge readout (6.5 psi @ max)
*keep in mind I still don't have a intercooler of any kind at this point, but I highly doubt that is the cause of these problems*

Ryshe
09-28-2002, 05:45 PM
Had to reply to myself to finish this up. Kinda ran out of character space on the last post....10,000 characters is the limit in case any of you wanted to know =).

So... as you can see... I am quite the frustrated person right now because I have poured countless hours of my time and friends' time, and poured out more cash than I could ever imagine...*** to try to get my car to run NORMALLY AND GOOD.

Tomorrow...er..today whenever I wake up, we plan on checking the timing again, which we have done before the first time I had my car back. We'll also be replacing the stock fuel filter with a 300zx TT fuel filter and changing the fuel pump fuse to one that is +5 amps more.

So bottom line, I feel like I have done and checked almost everything in my power to make my car run as it should, but now I bet it can barely stay within the 16's for 1/4 times.

If you've got a solution, suggestions, questions, go at it. The more people that respond to this post, the better.. as my friends and I are fresh out of solutions and energy at the time being.

-Tony '95 Gold 240sx

bonk
09-28-2002, 06:52 PM
I can't answer your questions, but I would post this in zilvia.net. When I had a 240 there was a lot of info on that site that was helpful.

NX-DET
09-29-2002, 01:11 AM
make sure that you have the correct o2 sensor in there.

i don't know too much about the 240's but i assume that they are the same as the b13/b14's

jwt ecu= usdm o2 sensor
stock ecu=jdm o2 sensor

civicdragon
09-29-2002, 01:37 AM
Take the shit back to boostfactor and have them give you what you paid for, a running turbo charged car

SR20steve
09-29-2002, 06:29 PM
I agree with civicdragon, you payed for a sr20det in good running condition they did not give that to you, period. It may be the motor itself so take it back to the BF people and tell them you arent going to give them anymore money and they need to fix it, whether it be fix something or replace the motor all together. Threaten to sue, its your car they are messing with.

Ben
09-29-2002, 11:56 PM
The most glaring fact that I see that makes IMO BoostFactor a shitty business is that they never even test drove the car to see if it ran right. If they went out and tested the car they would have seen there were many many problems and would have worked on them until they got it right like any reputable shop. What kind of shop would do ANY work to a customer's car, from changing the air filter to swapping an engine, would not go out and test drive to car to make sure the work performed was done properly and to make sure they didn't accidentally screw something else up in the process? Either that or they DID test drive the car, KNEW it ran like crap, and is now continuing to take advantage of you.

This shop is shit. You paid for a full swap, got car back, car doesn't run right whatsoever, overheats, etc. You take it back. They work on it more, and it still doesn't run right. I don't think you are going to get your car running right with these people. You could sue, but I'm not sure how successful you would be since you messed with the car a bunch yourself as well to try to fix it. If you are going to have a shop do something, then make them responsible for everything. Why should you try to fix it yourself? You just paid them to get you a great running DET powered 240. You did not get that. You should have IMMEDIATELY taken it back and said "This is shit. Fix it. NOW."

Regardless how you handled the situation, they are still at fault and you may be able to sue them still. They don't know at all what they are doing. I personally have never done a RWD DET swap, but you can be sure if I did I wouldn't hand the keys over until the car ran and ran well and reliably, no matter how hard or tricky it was.

PlanoSER
10-01-2002, 02:02 PM
last night we put a nice, big Greddy Front mount Intercooler on the thing and it still runs like garbage. To top it off, i think they (BF) sold him an i/c for an S13, when Ryshe has an S14.. nothing seemed to line up right but after some tweaking and customizing we got it all on there real nice and snug. I feel really bad for my friend Ryshe here and have been helping him work on his car till around 2 am every night the past week to get this thing workin how it should. The whole thing has just been one huge headache.

jon3k
10-01-2002, 03:15 PM
Is the car making any boost? When does it begin to spool? When do you make full boost?

Hien-eken
10-01-2002, 03:36 PM
i am almost positive that the car was NOT test driven (unless you consider a drive from the back of the shop to the front of the shop a test drive). keep me updated, Tony. - Hien

gfx2043
08-20-2008, 02:52 PM
you ever figure it out?

gfx2043
08-20-2008, 02:53 PM
ever figure it out?

b13kev
08-20-2008, 04:52 PM
ever figure it out?

wow.....epic thread revival......:squint:

vdubya63
08-20-2008, 06:10 PM
6 yr old thread..wowzers

swiss
08-20-2008, 07:58 PM
When searching goes bad.

budgetNX
08-21-2008, 03:28 AM
When searching goes bad.

geez tough crowd.

at least give him some credit for searching.

swiss
08-21-2008, 11:17 AM
I was just kidding about it. ;) If the original poster still has an email notification, he might respond, but....

Last Activity: 12-22-2002 10:38 PM

... not likely. :D

McCoy
08-21-2008, 12:34 PM
lockie lockie.